Tomorrow we start it. Dad is back in town and I really want another set of eyes here when we fire her for the first time. Too many things were modified. Need to look for leaks and keep fluids topped up while the cam is breaking in. Once she fires she needs to run for 15 minutes at 1500 rpms.
Over the last week I pulled both the front rotors off and repacked the bearings. You think your pickup truck's rotors are heavy? These weighed in at 64 lbs each. One side had been done before and the other was starting to show some wear, so they were replaced.




While they were off I ran them down to Les Schwab tires for a quick turning. They had never been turned before and were in great shape the guy said. Good, because they are getting hard to find.
In the box are new brake hoses that are waiting for my newly rebuilt calipers to be shipped in. Due here Thursday.


Since my back was still feeling ok, I decided to pull the rear drums and check the rear bearings. Those suckers are over 150 lbs. I used an atv jack to get them off. Brakes and bearings looked great, so it all went back together. I am also waiting for a new brake hose going from the chassis to the rear axle. The old ones were looking pretty tired.


This is how the old battery cables looked. Yes, I am ashamed.


This is how the new ones I had made up today looked. :clap


Of course, this is why I dont like anyone to work on my stuff. As I was installing them the cables just pulled out of the ends. The shrink tube was all that was holding them on. So I had to tear them all apart and solder them. What a PITA. I will be talking with the shop that did them tomorrow.




Finished:


Tomorrow she lives again. (knocking on wood)
Well, I got a story for you guys. I did get her fired today, but not without some pain and a lot of frustration.
She was all ready to fire yesterday. I did all my checks and all was right, well, they were not, but it would take until this evening to find the problem. She
would not even try to fire. No matter what I did, nothing. After a couple of hours I found that there was a glitch in the wiring of the new ignition system. The ignition wire I connected to that triggers the MSD ignition would go dead when the starter was cranking. So I fixed that and we had spark. Still no dice.
I pulled the carb apart, checked fuel pressure, rechecked that I had all my spark plug wires in correctly, I had the firing order right, etc., etc., etc. The only think that kept coming up was that I wondered if I somehow mounted the cam out of time.
It was not until this afternoon that I pulled the left valve cover and the distributor cap and starting at TDC of #1, rotated the engine and noticed that the distributor shaft was 180d out. I corrected issue and she fired to life.
Oil pressure is great and it never got hot running 15 minutes at 1500 rpms to run in the cam. Let her idle down after that and adjusted the carb and timing. She is purring now.
Tomorrow I finish the brakes as the new calipers showed up today. She should be on the ground tomorrow afternoon. I will get some photos and may even try a video tomorrow.
Something else I would like to fill you in on. I always have run Autolite plugs in the beast. They were easy to get and always ran good. Well yesterday when I flooded her so bad I decided to pick up a new set to install today.
I started to set the gaps and noticed that the ground electrodes were really off center. Upon closer inspection it was not the grounds that were off, the center insulator was off center in the bores. Then I noticed that distance that the electrode protruded out of the insulator varied by almost 1/8 of an inch. The more I looked the more problems I saw. Threads messed up, loose insulators in the metal bases, and cracked ground electrodes.
It was then I noticed the reason. “Made in China”. So much for Good US plugs. It took some calling around but I found the proper NGK plugs and the quality difference is huge.
The coach is done and had her maiden voyage. It was a short run into the hills so I was not able to check mileage, but power felt good. No more power than before, but the torque curve goes much lower in the RPM band now.
Braking is much improved as is the steering. Actually, the new steering is so light that it is almost too light. Looking at correcting that with a spring centered steering stabilizer made for coaches.
No smoke, no leaks, good oil pressure, cool temperatures even when pulling hard, all is well.
On our first major run since the major rebuild last winter. Couple of problems getting sorted out. Traveled with the wife, cats and a full load from Boise to Kellogg, Idaho. Pulled the Mercedes Benz ML430 SUV (heavy)
-Timing. Fought pinging problems really bad on the way up here. Did a bunch of research online last night and found out that having the vacuum advance on the ported vac is wrong. Needs to be on manifold vac for a situation like this. That way when I step into it and manifold vac drops and I go into a rich power mode, the vac advance backs off. (rich mixtures burn quicker than lean, needs much less advance).
Exactly the problem I was having. Too much advance under power.
-Fuel mixture too rich. Only pulled 5.5mpg. Should be around 6.5 under the conditions we drove in. I was hoping for much better, but I will settle for no worse than before the rebuild. We will see on the way home with the timing modification I just did and leaning the jetting out a bit.
-Generator quit just before arriving at camp. Looks like the points wore out. I replaced them and it is running again. I just need to fire it up under a load to adjust the carb a bit.
-New steering system and air ride suspension is great! Rides and drives fantastic.